MSP2003.5_Nick
Member
- :
- 2003.5 Mazdaspeed Protege - Dark Silver
I was driving on the highway at no more than the legal speed limit and was definetly not racing anyone at all. I did not downshift to third and continue at WOT midway through fifth. I was just driving along casually, doing nothing illegal in any way and it started misfiring and blowing blue smoke out the exhaust.
I pulled over and got it towed home and tore the motor apart and saw that piston #4 was broken. Sidewall of the sleeve is all scared up but I think the rod is still good cause the motor was still running smooth other than only running on 3 cylinders. It didn't make any big bangs or anything. I'm gonna take the rest of the motor out tomorrow and look it over see what else if anything is wrecked. The scarring is pretty deep, not sure if they can resleeve it or I have to get a new block. Head is still mint though.
This is what happens when you boost 22psi for 2 years lol, forged or not it's still a lot of abuse to take. I had Wiseco 9:1 pistons with 0.5 mil overbore and Eagle H-Beam rods.
I pulled over and got it towed home and tore the motor apart and saw that piston #4 was broken. Sidewall of the sleeve is all scared up but I think the rod is still good cause the motor was still running smooth other than only running on 3 cylinders. It didn't make any big bangs or anything. I'm gonna take the rest of the motor out tomorrow and look it over see what else if anything is wrecked. The scarring is pretty deep, not sure if they can resleeve it or I have to get a new block. Head is still mint though.
This is what happens when you boost 22psi for 2 years lol, forged or not it's still a lot of abuse to take. I had Wiseco 9:1 pistons with 0.5 mil overbore and Eagle H-Beam rods.
Last edited: